I have parted ways with the MGB, It was a fun learning curve.
Without a hiccup, it made its way down I-20 to Tyler, TX with its new owner at the helm. Godspeed sir.
Tuesday, July 18, 2017
Friday, March 17, 2017
Its alive (again) and running
Id like to thank sportscar parts ltd from Nashville for sending another*entire* set of pistons to replace the 1 piston that was the wrong size in the first order. Thats service. The rest were shipped back with a note of gratitude.
In retrospect i believe the original rings and pistons along with a maxed out timing chain adjuster couldnt keep up with the new found compression being created by the new head. Thus, the rebuild.
On to business:
Every thing reset to standard specs, static timed, hifs reset to stock plus 1 turn rich.... the key turned and it fired.
It fired for 5 to 10 seconds and with a timing light , adjusting the distributor, and a screwdriver she idled.
After getting a little heat the idle was raised to 1700rpms for a couple minutes to get everything friendly in the engine.
Depressed the clutch and took it for a gradual spin.
The engine is way more willing than it was before, I wound it up to 3000 a couple of times through the gears and took it back for a little tuning.
Its a happy car again and a joy to drive
In retrospect i believe the original rings and pistons along with a maxed out timing chain adjuster couldnt keep up with the new found compression being created by the new head. Thus, the rebuild.
On to business:
New little bearings copper head gasket, pushrods, head studs
----------------
So after spending 2.5 hours re installing,Every thing reset to standard specs, static timed, hifs reset to stock plus 1 turn rich.... the key turned and it fired.
It fired for 5 to 10 seconds and with a timing light , adjusting the distributor, and a screwdriver she idled.
After getting a little heat the idle was raised to 1700rpms for a couple minutes to get everything friendly in the engine.
Depressed the clutch and took it for a gradual spin.
The engine is way more willing than it was before, I wound it up to 3000 a couple of times through the gears and took it back for a little tuning.
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